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Silver State Helicopter Down south of Jacksonville


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Just to set the story straight, my sister Tamara Williams died (as well as her student Wyatt Duncan) because of Silver State Helicopter's lack of safety protocol conducting a routine maintenance on the R44. She wasn't scheduled to take that particular helicopter, but because of SSH management's chronic scheduling mistakes, Tamara and Wyatt went up that day and never came back. Anyone who went up in that R44 was certain to die - the faulty work was covered by a plate and it was impossible to detect on any preflight inspection.

 

But don't take my word for it, read the full NTSB report here:

http://www.ntsb.gov/ntsb/brief.asp?ev_id=2...00374&key=1

 

The Probable Cause Report:

 

NTSB Identification: DEN07FA079.

The docket is stored in the Docket Management System (DMS). Please contact Records Management Division

14 CFR Part 91: General Aviation

Accident occurred Tuesday, March 27, 2007 in Ponte Vedra Bch, FL

Probable Cause Approval Date: 1/31/2008

Aircraft: Robinson R44 II, registration: N744SH

Injuries: 2 Fatal.

 

The local instructional flight was scheduled for a east departure from the airport and a flight south along the coastline. Several witnesses observed the helicopter approximately 200-500 feet above ground level (agl) in cruise flight along the coastline on a south heading. One witness, a former pilot and mechanic, reported he observed the helicopter in straight and level flight, then heard a change in "rotor noise, followed by a bang/pop/twang sound." The helicopter then "snap-rolled" to the left and descended into the terrain in a nose low attitude. Examination of the helicopter's flight control system revealed that the right forward servo to swashplate push-pull tube joint was disconnected and the attach hardware (bolt, lock nut, two washers, pal nut) was missing. The left forward servo to swashplate push-pull joint was connected; however, the nut was found partially engaged on the bolt threads, and the torque was "finger tight"; no pal nut was noted. Material analysis of the components revealed that only one of the two nuts for the left and right connections were installed, and then only finger tight. The nut on right servo connection rotated off during flight which allowed the bolt to extract itself and disconnect the servo from the push-pull tube. Prior to the accident flight, an inspection, which required the push-pull tubes to servo connections to be disassembled, was performed on the helicopter, and a 0.5-hour maintenance test flight. The mechanic who preformed the inspection, stated he forgot to properly secure the hardware for the left and right servo connections. The mechanic stated the reasons for the error were the following: 1. He was pulled," in all directions" by company personnel since his arrival at that facility; 2. The "reassembly was not opposite of the disassembly," which was a personal maintenance practice he used to eliminate errors; 3. Two nights prior to the completion of the inspection and the maintenance test flight, the apprentice providing assistance, wanted to stay late to finish with the mechanic a certain section of the inspection. As a result, the mechanic forgot to go back and secure the hardware connecting the two push-pull tube to servo joints; 4. The company was understaffed with maintenance personnel. According to the company's maintenance quality control program, any maintenance completed on a helicopter was to be inspected by another mechanic. A review of the program revealed that the mechanics were not following the program, and the company was not providing oversight and enforcing the program.

 

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

the mechanic's improper installation of the attachment hardware for the servo to swashplate push-pull tube joint which resulted in a disconnection, subsequent loss of control, and impact with terrain. Contributing factors were the company management's inadequate surveillance and enforcement of maintenance procedures, the excessive maintenance workload due to inadequate staffing of maintenance personnel, and the insufficient management of maintenance tasks.

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Shannon- we are all sorry to hear of this loss. There have been other discussions about this incident just after the NTSB released its findings, and of course, now...there are very few posters left that will defend any of SSH actions. This was clearly a mechanical error with devastating results...this should never have happened.

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  • 4 weeks later...

Shannon: Thank you for posting information about the accident/the accident report. Wyatt was one of my best friends, and though it's been nearly a year since the accident, it's been difficult to accept what's happened. I take comfort in at least knowing why the accident occurred, but it is painful to realize it is something that could have been prevented. I am so sorry for your loss. Not a day goes by that I don't think about him and this accident.

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